Vehicle details: | Lotus |
Year: | 2004 |
Symptom: | Engine misfire (intermittent), MIL on, P0201 |
Author: | Nick Hibberd | Hibtech Auto-Electrical Diagnostics |
The vehicle had an intermittent misfire and the engine MIL was on. I found the engine misfiring constantly, with excessive smoke issuing from the tailpipe, so I left it running for a little while to get a feel of the problem and to scan the system for trouble codes. I couldn’t keep the engine running for too long because the hydrocarbon (HC) content in the smoke was unbearable. It was immediately clear that this wasn’t a normal misfire, and there were a few causes for concern:
The scan tool showed only one diagnostic trouble code (DTC) logged — P0201 INJECTOR CIRCUIT MALFUNFUNCTION CYL NO.1
This type of code is a big help because it’s specific to a component and is directly related to an electrical problem. The dreaded codes are P030#, which relate to general engine misfires, but I could list probably 20+ different reasons that will cause a misfire and these DTCs to become logged, so this is not much of a help. Also, we only have one DTC logged, which is another clue. Several attempts to erase the DTC failed, with the code and the engine MIL coming straight back on. So we know the fault is permanent, we know the offending cylinder, and more importantly we know the offending circuit.
It’s time to hook up the scope.
Here we have the scope and low-amp clamp measuring current drawn from the main 12V+ output from the relay module to various engine components. In this case we are interested only in No.1 injector circuit, but from this test location we could build a bigger picture of the fault by including all injectors.
Capture 1 shows a collection of electrical loads that this particular 12V+ source is supplying. Unfortunately, whilst I was gaining access to the relevant cabling and connecting the scope, the fault went away and the engine started firing again on all four cylinders. This was a big clue. When connecting a scope, some cable and connector flexing is inevitable, so it must have been this that disturbed the fault. The capture showed typically good signals, with all injectors firing and coil signals to match. But which one is our No.1 injector? Well, this capture offers no indication which is which, but we can deduce that no abnormal activity exists.
Each signal trace was examined for general integrity, and no abnormality or inconsistency was noted. This is just what you would expect from a sound running engine.
Only one of the scope’s channels was used, leaving an option to synchronise the current trace with a known firing command. The obvious choice would be to view our suspect No.1 injector negative line. I chose not to use the No.1 injector ground command as a sync, for fear of losing the fault completely due to flexing of the cable and connector. I felt confident that the fault was severe enough to be spotted through the current clamp in one form or another.
Because we suspected that a cable flex affected the fault, the entire engine bay wiring harness was subjected to a “wiggle” test in attempt to flush out the fault. When using this technique, always start out very gently. Wiring harnesses throughout the car are all subjected to driving vibrations and knocks, very often just around one particular point.
It’s here where your fault is most likely to be, so it’s no good yanking and pulling on the harness, because the fault you are investigating didn’t have to be yanked or pulled in the first place for it to become a problem.
It didn’t take long before the engine stumbled and kicked out smoke. Capture 3 shows the result.
We see a missing injector current trace which has to be our No.1 injector. A missing current trace indicates that injector isn’t working, but this makes it hard to explain the massive HC level at the tailpipe. The capture also shows the minimum current from capture 1 at 1.4 A raised here to 2.3 A; a difference of 0.9 A. Can this be a coincidence?
This is an excerpt from capture 1 showing known good injector traces. This one has been zoomed in slightly to get a better look. Each injector is seen to saturate at approx. 0.937 A.
This fits nicely with the injector winding resistance and engine running supply voltage.
Charging voltage 14 V
Injector resistance 15 Ω
Current draw 0.93 A
The facts so far are all pointing to a short to ground in the switched negative supply line to No.1 injector.
In Capture 4 we see the distinct difference between fault present and fault absent.
Finding our short to ground turned out to be easy. Each segment of wiring harness between ECM and injector was carefully flexed until one area stood out as being strongly related to the fault. I could get the fault to appear at will as if flicking a switch.
For this part of the investigation I only needed the ignition on, and I could hear the injector working as I flexed the harness.
This photo shows one part of the engine harness which runs to a block connector under the throttle housing and carries all injector and relevant cabling. When this connector block was gently moved, our fault would appear.
I switched off the ignition and disconnected the block connector for a closer look. All terminals seemed OK and well secured. A problem inside the connector housing didn’t fit the fault; this might perhaps cause an open circuit condition where the terminals don’t quite meet, but not our condition where we are looking for a short to ground.
I traced the problem to just the other side of the connector block. The negative command line to No.1 injector had chafed on the underside of the throttle housing. Incidentally, you can also see in the picture where the original harness protective tubing starts; the short length of unprotected wiring from the connector to the tubing was enough to allow the cable to stray and chafe.
None of the cable strands had been damaged, so I simply had to re-insulate and reposition the cabling.
This had been an intermittent problem for the customer for some time, and as a result the engine oil had suffered by being saturated with raw unused fuel. When the vehicle was taken for a run to settle things down, the fuel trim was up into double figures trying to back off the injection duration. The crankcase ventilation was channelling the HC held in the oil back into the inlet plenum.
To put a final touch on the car, I replaced its oil and filter.
Donald Gamble
August 31 2014
Thank you, Nick.
Anonymous
December 02 2013
Hate to say it but alot of dealers just don’t care to fix these problems. Just through parts at it!
Salvador
September 02 2013
Very good explained step by step a lot to learn I recently bought a pc based 8 channels scope I AM learning a lot on these articles
Steve
January 08 2013
Excellent diagnosis,faults like this can be very difficult to find without the correct equipment,information and most of all knowledge,great reading and a big well done on fixing the issue
Bancroft
October 07 2012
Great article, a CAT performance test would top this off… great job man!
resarias
July 17 2012
Great case study, I think that in a case like this the car will need a new catalytic converter as well
Ruben C
March 29 2012
Written and illustrated with great clarification.
Thank you for your service.
Lee A.
January 01 2012
lovely job,good thinking and patience to fix a complex issue and without replacing any part.
Harold Carbajal
November 24 2011
Thank you for this very indepth explation, good work!!
Javier
August 23 2011
A fault that shows a lot about an engine malfunction and a lesson to learn a lot.
Geoff T
July 27 2011
Man what a Great case Study
W Mills
November 03 2010
I own a 2002 ford renger xlt 2.3 engine. I have had it in the shop for at least ten times for a misfiring one # 1 cylinder, the dealerships have been unable to find the cause and correct the misfiring.
john ball
March 08 2009
very interesting article - I am experiencing a similar mis-fire on my 740il and there is no fault with the coils or O2 sensors. The system is mis-firing and CO levels are very high. Will evaluate for an injector fault.